张琪,李宁,靳艳智,王孝义.液压作动筒复杂双油路腔流量偏小问题 仿真分析及验证[J].航空发动机,2018,44(6):
液压作动筒复杂双油路腔流量偏小问题 仿真分析及验证
Simulation Analysis and Verification of Small Flow Problem in Complex Double OilCavity of Actuating Cylinder
  
DOI:
中文关键词:  液压作动筒  流量偏小  数值仿真  可调喷管  航空发动机
英文关键词:hydraulic actuating cylinder  small flow  numerical simulation  regulated nozzle  areoengine
基金项目:航空动力基础研究项目资助
作者单位E-mail
张琪,李宁,靳艳智,王孝义 中国航发贵阳发动机设计研究所贵阳550081 airmen_es@163.com。 
摘要点击次数: 1353
全文下载次数: 960
中文摘要:
      为解决航空发动机可调喷管液压作动筒工作腔流量偏小问题,对作动筒复杂双油路腔开展了CFD 数值仿真分析,阐明 了作动筒流量偏小原因,提出了增大流量的措施并仿真分析了改进效果。计算结果表明:仿真流量由465.5 mL/s 增大到539 mL/s, 增大了73.5 mL/s;流量实测值由443 mL/s 增大到507 mL/s,满足设计要求,最终通过作动筒流量试验验证。
英文摘要:
      In order to solve the problem of small flow in the working chamber of regulated hydraulic nozzle actuator of aeroengine, CFD numerical simulation was carried out for the complex double oil cavity of actuating cylinder,and the reasons for the small flow of actuating cylinder were expounded. The measures to increase the flow were put forward and the improvement effect was simulated and analyzed. The results show that the simulation flow increases from 465.5 mL/s to 539mL/s and increased by 73.5mL/s;The measured flow which meets the design requirements is increased from 443mL/s to 507mL/s. Finally the flow test of the actuating cylinder is verified.
查看全文  查看/发表评论  下载PDF阅读器